Saturday, January 27, 2018

Saxaphone ligature screw


Edwin's saxaphone ligature takes two 6-32 screws.  One of them broke, so I made a replacement.  I started with 1/2" diameter steel rod.  I think it was zinc plated, but that wasn't too critical; whatever plating was originally there was removed.

I started by turning the portion to be threaded to 1/8".  Since the length wasn't too critical, I just used the good screw to figure the length.


I threaded the end by hand.  (I could have used a geometric die, but the setup would have been longer...)


Once threaded, I turned the shoulder that separates the threaded portion from the handle.


The shoulder actually tapers a bit, which I did with the graver.



The handle is a rounded ball, which I shaped with the graver after using a parting tool to remove most of the waste.

Here is the part next to the broken screw after parting.


I removed the leftover spigot by reversing the screw in the lathe -- good thing I have an 1/8" collet.


Now the handle is ready for final shaping.


Since I had to remove lots of material, I figured I could either spend time with a file or the bench grinder.  The bench grinder seemed like the better option (it may not have been any faster, actually).  I gripped the part in a pin vice so that I was securely in hand.


I ground both flats with numerous breaks to dunk in cool water...


After polishing, hardening, tempering, and final polishing, here is the final product in place.


The handle is a little wider than the original, but it does the job.

Monday, January 15, 2018

80 meter antenna

We built several Cricket 80a kits, which operate in the 80 meter amateur band.  Since we don't have any antennas specifically for this band, I decided to make one.  The design is a basic dipole fed with coax and a current balun at the feedpoint.

Here are the feedpoint parts: 


The coil is bifilar wound with 13 turns of 22 AWG speaker wire through a toroid.  It measures around 350 microhenries.  The extra loop is for a support cable to lift the feedpoint.  The enclosure is a watertight plastic container that has holes drilled for the SO-239 connector and mounting hardware.  I found that it was easier to control the drilling by hand (rather than by power drill), and a step drill made the holes cleanly deburred.

The two wires attach to the coax center and shield, while the other leads attach to the antenna.  It made sense to do the electrical work first...


... and then install it in the container.  I applied plastic epoxy to each of the pass-throughs before installing hardware in an attempt to seal out any water.  After the hardware was installed, I screwed in the antenna connections tight.


Here is the final enclosure, ready for the radiating wires.


Connecting from the hooks to the radiating wire segments is done with a short feeder segment of stranded wire.  Loops are soldered in the stranded wire while it's installed on the enclosure.  To avoid melting the plastic, I gripped a hemostat onto the plastic side of the junction to draw the heat.


Here are the feeder segments ready for the radiating wire segments. 


The next step was to design the radiating wire segments.

For the radiating structure, we are constrained by the feedline length (25 feet of RG-58) and the confines of our lot.  We're lucky that the antenna basically runs the length of one side of our property, basically touching the ground on one end due to ground slope.  Here is what NEC seems to suggest:
  • Height of antenna above ground: 2 meters
  • Length of each leg: 20 meters = 65 feet
Here is the impedance and VSWR according to NEC:


Here is the radiation pattern according to NEC, which clearly indicates that the main beam is vertical, which should be good for near vertical incidence skywave (superimposed on the antenna structure):


Given this plan, I measured out two runs of 67 feet each; better to cut long and trim than the other way around.


The wires are attached to the feeders.


Ready for installation!


Then I strung the works into position.  This took a while; after trimming off the excess wire, I got a near perfect SWR around 3.560 - 3.580 MHz, right where I wanted it.  As NEC predicted, the antenna seems to degrade higher in the band, with a 2.5:1 SWR around 3.800 MHz.

Thursday, January 4, 2018

Extreme IC repair

For Christmas, our family of hams got Cricket 80A transceiver kits.  They are not terribly hard to assemble and are good soldering practice. 

One problem we had with two of them was that the local oscillators did not start up.  It turned out that the 2N7000 MOSFETs are susceptible to electrostatic discharge (ESD) damage.  For whatever reason, the Q1 local oscillator transistor seems more vulnerable to this.

But in one of the kits, there was a problem with the audio amplifier IC, an NJM-2113D.  In the process of soldering and apparently removing, three pins broke off.  These are not exactly standard, at least they're not in my junk box. So although I put in an order for a replacement, Donna pointed out that I could probably fix it anyway.

The issue is that pin 1 (GND) broke off at the case, so I set about using a four fluted 1/8" endmill to cut the case to expose more of the pin.  I gripped the endmill in a collet in the headstock of my lathe.


My biggest concern was part-holding.  Fortunately, I was able to grip the IC in a toolpost, which also didn't break it.


After a few passes, I successfully exposed what seemed like enough of the pin to take solder.

I started by soldering the intact pins to the board and then the third pin, which was broken off, but not all the way at the case.  For this, I ran a piece of tinned copper wire through the hole, soldered it to the board, and then to the IC.


Then I ran another piece of tinned copper wire through the hole for pin 1 until it stopped on the exposed part of the IC, and soldered it to the board.


Finally, I soldered the new pin 1 to the IC.  I used a bit too much solder, but it's a good connection.


And, it works!  Here is the happy owner of the completed radio.